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Problems
If you've been following the timeslip log, you probably noticed that our last trip to the track, back in May, left us scratching our heads. After running a string of 12.0's during our March outing, and knocking off stellar sixty-foots in the 1.60's, the May outing was a huge disappointment; the car would not hook up, the engine was running rough, fouling plugs and backfiring. All in all, we could barely get the car into the 12.30's. So we spent the last month trying to figure out what was causing the poor performance. The problem seemed to be a really lean condition between 2500 and 3500 rpm, causing severe popping and backfiring out the exhaust, almost as if a rev limiter was being applied. However what complicated the problem were fouled plugs at cylinders 1,4,5,8. Typically with a single plane intake and we'd expect to see those cylinders slightly leaner, since the runners are the furthest away from the plenum.

We suspected the problem was either in the carb or in the distributor. Swapping out distributors, playing with timing curves, replacing plugs, wires, cap and rotor yielded nothing. Rebuilding the 750 double pumper, twice, did not help. Trying no fewer than two dozen jet, powervalve, and shooter combinations, did not change a thing. Thinking the problem may be in a metering passage, we swapped on a 650 double pumper.... nada. Finally we tried the Barry Grant 750 from our Project FE car. The problem seemed to be gone. Throttle response was back, there was no stumbling or hesitation.


We hypothesized that this top of the line Silver Claw carb is probably less affected by a poor vacuum signal from the single plane and large duration camshaft. However this doesn't explain why our 750 Holley worked so well during the first two months on the motor. Needless to say we are still perplexed. The next step will be to have the 750 professionally rebuilt. Perhaps there is something stuck in one of the metering passages, that for some reason we can't get out. Anyway let's get to the point....
Back to the track
Feeling that the Barry Grant carb was working well we decided to make another shot at the 11's. The FORDMUSCLE crew (Jim Langley, Victor Silva, and myself) set out for Sacramento Raceway. I made a couple of shakedown runs to get a feel for the track and how the slickswere hooking up. The car immediately knocked off a 12.27 at almost 116. Seeing the mph back over 115 was a good sign, especially since the air temp that evening started out at a balmy 85 degrees. However it seemed that we still had a traction problem. After two runs our best sixty foot was a 1.80 -an eternity away from the 1.60's we were expecting. Launching at 4000 was still breaking the tires free, resulting in having to having to back off the throttle until they hooked. Perhaps the ET Streets were starting to show their wear, after all we had made over 150 passes on them.

We decided to drop the tire pressure down to 10 psi as this would offer more sidewall wrinkle, but at the expense of some high speed instabilty....I'd just have make sure to keep the car pointed straight!

The car responded to the lower tire pressure, with short times dipping into the low 1.7's. Combined with the lowering air temperatures (now in the mid 70's), the car was really starting to move like it's old self. We now had back to back runs in the low 12.1x range, with mph still over 115.

At this point I felt that for whatever reason we were not going to get the sixty foot times into the 1.6's. The car simply did not want to hook like it used to. We had tire pressure set absurdly low, and even then a 4500 rpm launch was breaking them free. Victor was under the car earlier and seemed to notice that the axle spring perches and u-bolts were bent, possibly causing a change in the pinion angle -which would defiantly hurt traction.

Nevertheless we were very close. All we needed was a tenth. If we weren't going to get it from the short times, then the only other place we felt we could improve was in the shifting. Knowing that I am not the fastest shifter, I turned the keys over to Victor Silva. Victor simply has more experience and more confidence in powershifting. Besides, I had not had a chance to stand back and actually watch and listen to this car run. We have received many compliments on how intimidating the car sounds with the Terminator exhaust system, so I figured this was a good opportunity to hear it for myself.


Victor makes a pass
After getting familiar with the cockpit, Victor pulled the '67 to the line, did a quality burnout, and staged against a blown late model 5.0. I was standing behind the wall at about the 60ft mark, trying to get a couple of pics as he launched. Before I could even pull focus with the camera both cars roared by me. I quickly turned around to look at the light board, and saw what I thought was a 1.87 sixty foot time -but it could have been a 1.67, I couldn't tell for sure. The next thing I saw was both cars breaking the traps at approximately the same time. The blown 5.0's ET flashed up as a 11.83, but immediately after our lane lit up with a 11.98!
Wow, Victor did it! I was absolutely stunned. What a rush! I walked over to the tower to get the timeslip, and sure enough Vic managed a 1.67 sixty foot, combined with blazing-fast shifting, and got the Project car to beat its goal. [see timeslip]

So what's next for Project 11.99?
Well the car is still a ways off from running consistent high 11's. Running 11's poses a whole laundry list of changes when it comes to NHRA regulations. Primarily we'll need a four point roll cage and a scatter shield. However the added weight would probably keep the car in the low 12's. What we will probably do is pull the heads and do some extensive porting and try to gain thirty or so rear wheel horsepower. Remember these World Sr. heads have nothing more than a quick cleanup. The goal will then be to run consistent 11.80's-11.90's, along with meeting the NHRA safety requirements. Look for future articles on the head work, scattersheild and roll cage installations, and of course more trips to the track.

Key Points about Project 11.99 and 400 Horsepower 302
From the beginning our goal with both projects, has been to show you the readers that it does not take much, in terms of exotic and expensive parts, to build a streetable 11 second car, powered by a naturally aspirated 302. What it does take is the proper combination of parts; both chassis and engine. We're not saying that our projects are the easiest way to run 11's, or even the most streetable. Of course there are arguments to be made for nitrous and blowers, as well as larger displacement. However one thing that cannot be beat by power adders is the jaw-drop and disbelief of people when you tell them your running 11's with a naturally aspirated 302 on pump gas. F/M

"Highlights" and causes of disbelief
- Small block 302*
- 9.4:1 compression
- 89 octane (even on the 11.98 pass.)
- Fully muffled exhaust.
- Stock 1989 T5 transmission
- 8" rear end
- Stock 28 spline axles (we did break one.)
- Weight with driver and fuel: 3280 lbs.

400 Horsepower 302 - Reciepts
Used block: $50
Machine work/balancing: $500
KB Pistons: $250
World Sr. Heads (used): $600
Vic Jr: $200
Crane Solid Roller cam/lifters/springs: $700*
Misc parts (main studs, windage tray, etc.): $400
Total engine cost approx. $2600*.
Not including incidentals, such as gaskets, fluids, etc.
*Significantly cheaper if you substitute flat tappet solid cam of same specs.
For detailed build up, see 400 Horsepower 302 buildup articles.

Project 11.99 Series
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