DIY EFI Part II - continued
Shortly after publishing Part I of DYI EFI we completed
the exhaust work and fired up the motor. The initial reaction
was all smiles. The motor fired up on the first turn of the
key - one of the immediate benefits of fuel injection. Even
more astonishing was that the engine idled with our relatively
lopey (226/232 degrees duration and .572 lift) non-EFI designed
camshaft. Unfortunately the celebrations were short lived
as the first of our problems came as the engine came up to
operating temperature. A large pool of coolant developed under
the engine and forced us to shut the engine down. A quick
inspection revealed the Cometic headgaskets were leaking -
a problem not uncommon with multi-layer steel (MLS) head gaskets.
MLS gaskets require mirror like surface finishes on the cylinder
head and block deck to seal up properly. Any slight surface
irregularities are channels for water to seep out of when
pressure builds in the cooling system. We took our chances
using the gaskets since we were not about to pull and disassemble
the motor to have it resurfaced. So the final score was MLS
gaskets 1, FordMuscle 0. We succumbed to more downtime and
eventually replaced the headgaskets with standard Fel Pro
graphite coated head gaskets (part number 8548 PT1).
That's not oil an oil leak but rather coolant. The Cometic
head gaskets unfortunately didn't seal up resulting in
a water leak between the rear coolant passage. |
We thought installing Cometic MLS head gaskets would be
a wise decision since we ultimately planned to reinstall
the supercharger. Unfortunately these gaskets require
a freshly machined mirror-like deck surface to seal properly.
We gambled, and lost, using them as a replacement gasket. |
By the time we got the head gaskets replaced and were ready
for our second try at proving the EFI conversion our appetite
to drive Project 67 was voracious. We hadn't taken the car
to track in over six months and were getting antsy watching
the summer evening track sessions pass us by on the calendar.
With a turn of the key the inline fuel pump primed and the
engine came to life with the swiftness and predictability
we expect of fuel injection. At operating temperature we confirmed
the replaced headgaskets had solved the coolant leak problem
and we were looking to be in good shape for the first road
test. After easing it down the street to the first open section
of road we slowly started bringing the rpms up. The throttle
response was crisp and acceleration smooth up until 3,500
rpm. That's when the engine acted as if it was hitting a rev-limiter
and popped and sputtered. A couple more tries in different
gears confirmed that we had a fuel or ignition problem rearing
it's ugly head at exactly 3,500 rpm. Defeated again we rolled
back to the garage for more troubleshooting.
Fuel Pump Cavitation
One of the things we noticed after our initial test drive
was the inline fuel pump had gone from virtually inaudible
to a shriek so loud that it could be heard over the exhaust
system. Since this was such an obvious change in characteristics
we suspected fuel pump failure or cavitation as being the
likely cause of our 3,500 rpm engine cut out problem. Cavitation
is a condition when a liquid, in this case fuel, vaporizes
at the pump entry and forms voids or cavities of air. As the
bubbles collapse they release energy and force pressure against
the pump rotors.
Cavitation is generally is due to fuel temperatures getting
too hot or too low pressure feeding the pump - both condition
affecting the vaporization point of a liquid. The loud whining
sounds and drop in fuel pressure are signs of cavitation and
require correcting for proper operation. We suspected that
our pump cavitation was due to too small of a filter before
the pump. The 40 micron filter, while perfectly able to prevent
the smallest of contaminants from entering the pump, proved
to be too small to allow enough fuel to be drawn through at
the rate required by the pump. We changed to a 100 micron
filter, which also has a significantly larger filtering area,
and that solved the cavitation problem. Our hopes were raised
that we were finally ready to roll.
We learned that the inline fuel pump was cavitating due
to the insufficient pre-filter area (top), causing a pressure
drop before the pump and thus heating up the fuel. We
swapped to a larger filter with a cartridge element. This
cured the cavitation problem and made the pump whisper
quiet. Note that the larger filter uses a 100 micron filtering
element while the smaller is 40 microns. |
The fuel system consists of a Mallory 255lph inline fuel
pump with 100 micron prefilter and 40 micron post filter.
We modified
the stock sending unit with a -8AN fitting and ran -8AN
hose to the fuel rails. -6AN line returns fuel back to
the tank. |
Back to Basics
Perhaps it is a variation of Murphy's Law, but one of the
lessons that always seems to repeat itself regarding automotive
problems is that it will either take a very long time to find
the simplest problem, or that it will take no time at all
to find the most complex one. We're certainly headed that
way with our Project '67. We would never have suspected cavitation
had it not been for the horrendous sounds emitted by the pump.
So while the fuel pump is now quiet and pressure is constant,
we still have the engine breaking up at 3,500 rpm. In hindsight
we should have suspected ignition but then we would be dealing
with the cavitation problem now.
So at the time of publishing this article we've gone through
just about every ignition component except the spark plugs.
We've swapped out, for trouble shooting purposes, the plug
wires, distributor, TFI module, coil and computer. The problem
still exists and all that remains now is to pull the spark
plugs and check for a cracked insulator or perhaps a collapsed
plug gap. We know, some of you are wondering why we'd save
for last something as easy as pulling and checking eight spark
plugs. The answer - remember those Dart heads with the goofy
plug angles? It turns out you can't get a spark plug socket
over the plugs without removing the headers. It's an example
of how great design is worthless without basic functionality.
There, we've revealed to you our shortcomings. While we don't
expect to set any trends in the world of automotive enthusiast
media at least you know FM isn't sugar coating these projects
to make you think we have some superior skill sets you don't.
We're certain that this problem will be resolved soon, and
when it is we'll be back on track with dyno testing and installing
the supercharger.
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