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Boost Gauge
Text and Photography by Chirag Asaravala

The moment of truth has arrived. We have initial dyno results on our blown and stroked 1967 Mustang. Before we delve into the numbers here is a recap of the events which brought us to this point. Earlier this year we picked up a used Vortech S-Trim 5.0L Mustang supercharger kit. We spent a couple of months, working at a snails pace, trying to figure out how to adapt the kit to our carbed 331 motor and '67 Mustang engine compartment (see Part I: Mock Up.) Once all the mounting issues were sorted out we bolted the blower on for good and plumbed all the ducting. Part II cumulated in the firing of the motor with blower attached. Days after you read and heard the symphony of blower whine and lumpy idle (see Part II: The Pressure Mounts) we took the '67 out for its' maiden voyage under boost. As expected we were faced with detonation. We knew this would be an issue to contend with due to the 10.5:1 compression ratio of the 331. We tackled these issues, as you'll see later in this article, but before that we took the blower belt off and drove the '67 up to the dyno for some naturally aspirated pulls.

Naturally-Aspirated Dyno Results
The 331 stroker engine which was built nearly two years ago (see Build a 302 Stroker) has been a stout performer in naturally aspirated form. The '67 Mustang has gone as fast as 11.6 @ 119 mph with only track side tuning.
Needless to say we were curious to learn what sort of power it was laying down. We drove the car up to our local Dynojet facility, Advanced Dyno in Suisun, CA, and arranged for a three pull baseline session. We made an initial pull with the engine in the same tune it was when it ran its' best ET. It put down 356 horsepower at 6100 rpm, but the graph showed some important shortcomings (see blue curves below.) The air-fuel ratio (AF) was way rich at wide open throttle. On a naturally-aspirated engine we like to see AF between 12.5:1 and 12.75:1. On our initial pull we were at 10.0:1 from 5000 rpm onward. That's not only detrimental to fuel economy but to power as well.

Dyno Results (RWHP): Naturally Aspirated, 331cid
  Peak Horsepower Peak Torque (lb.ft)
Initial 356.9 @ 6100rpm 343.4 @ 4700rpm
Best 372.2 @ 6100rpm 346.2 @ 4900rpm


On the subsequent two runs
we started to jet the 750 Holley downward. We had started with 74's in the primary block and 79's in the secondary. For run two we brought the secondaries down to 75. The engine actually responded with a loss in horsepower, from 356 down to 350 at peak. Air-fuel ratio came up slightly, but still terribly rich at 11:1. This is an appropriate place to make an important point about dyno tuning, especially when dealing with air-fuel ratios and jetting. Carbureted engines will often times appear to respond unfavorably to a jet change. We were running rich so one would think a drop of four jet sizes would shown a power gain. In fact we lost power. This could easily have been interpreted as a sign that we were headed in the wrong direction. Fortunately experienced dyno operators H.H and Mike at Advanced Dyno have seen this all too often and know that the basic principles of engine tuning do not change from motor to motor. You have to press on. The AF ratio was still rich and engines simply do not make their best power with that much fuel.

We took another 4 jet sizes out of both the primary and secondary sides. With the carb now jetted at 70/70 we made our last pull. Low and behold the engine responded as expected and power went up across the rpm range, with peak now at 372 horsepower (orange curves in the above chart.) Air-fuel ratio could still be improved upon still hovering in the low 12's.

While we were thrilled to find new power in our naturally-aspirated motor we knew our ultimate goal was to get this motor dialed in for the blower. We were also detecting signs of valve float, evident by the sharp and choppy power drop right after peak horsepower. While not visible in our graph above the original power curve falls hard after 6100 rpm. We think this cam should be pulling a few hundred more rpms. We suspect the valve springs require replacing. Something we'll address in the near future.

For now we're packing the car up and taking it back to the shop. We'll bolt up the blower ducting, connect the belt, and prepare for some boosted dyno runs. (Continue)
(Dyno Results - Supercharged)
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In This Article:
Our Project '67 Mustang, now sporting a Vortech supercharged 331 engine, gets initial dyno numbers.


Also See:
High on Carbs Part I: Mock Up
High on Carbs Part II: The Pressure Mounts

 

Supercharged 331 stroker packed in the '67 Mustang bay. It took work and creativity but the power gains were worth it.
























Behind the Boost Gauge

To monitor boost we selected the Autometer Pro-Comp 2 5/8" boost-vacuum gauge (PN: 4477). We also stepped up to matching mechanical oil pressure and water temp gauges.

The boost gauge uses a MAP (manifold absolute pressure) sensor to convert vacuum/boost pressure into electronic signal. It features peak recall and a max-boost warning LED. The sensor requires finding a 12V key-on source that does not cut out upon cranking.

We located the MAP sensor under the dash and behind the firewall in our '67 Mustang. The vacuum tube connects to manifold vacuum (we used the full-time vacuum port on our Holley carb.)
Source:
Autometer

413 West Elm Street
Sycamore, IL 60178
Tel. (815) 899-0800
www.autometer.com

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