By C.Asaravala
If you were anywhere near Northern California the last week
of September you probably heard a big whooshing sound at about
noon on the 29th. That was my huge sigh of relief as our Project
'67 Mustang was unstrapped from the dyno rollers. Nearly six
months after embarking on an EFI conversion project we finally
had a running car - and one that runs surprisingly well too.
It all began back in February when we decided to ditch the
carburetor and install a Ford EEC based fuel-injection setup
from Mass-Flo EFI. We had grown tired of trying to tune the
carburetor to run with the Vortech supercharger we had installed
late last year (see the "High
on Carbs" series) . We knew that for ultimate tuneability,
and driveability, we'd have to convert to a computer controlled
system whereby we could infinitely adjust timing and fuel
delivery.
Mass-Flo's stealthy EFI system
is based on hiding the mass-air meter in the air cleaner. |
It didn't seem like too tough of a job. As we detailed in
Part I,
the conversion can really be broken down into three main sections
-fuel system, electrical and hardware. The Mass-Flo kit comes
with a custom wiring harness for early Mustangs (you could
use a harness from a 5.0L donor car but you'd have to deal
with unnecessary emissions sensors, etc.) With the harness
and computer in place we installed the carbureted Victor Jr.
manifold, modified for fuel injectors. On top of it goes the
throttle body and Mass-Flo MAF sensor. It's a pretty slick
setup that allows use of a standard air-cleaner giving the
impression of a carbureted motor to the unsuspecting eye.
Unfortunately we hit some turbulence in what otherwise seemed
to be a very straightforward path to EFI. As we reported in
Part
II the motor fired up immediately and the computer had
no problem idling the somewhat aggressive cam. The problem
reared it's head when we tried to drive the car. At 3500 rpm
the engine would hit a wall. In fact it felt so much like
hitting a rev limiter that I checked the car and engine bay
several times to see if there was some rpm limit module that
I had installed and forgotten about. The solution wouldn't
be that easy.
We spent every available hour trying to troubleshoot fuel
and ignition. Over the course of a month we swapped out the
MSD box, coil, distributor, plug wires, plugs and even the
computer. No change - run the motor up in neutral or in gear
and it would break up at exactly 3500 rpms every time. We
initially thought we were on the right track having identified
cavitation in the fuel pump (see Part
II for details). We tracked the problem down to a insufficient
filter size before the pump which was restricting flow. Unfortunately
swapping the filter out to a larger one didn't resolve the
3500rpm breakup, though it did resolve the cavitation.
Reaching out to the masses
That's where we left off in the last issue. We suspected at
this point that the problem had to reside in the wiring but
we weren't sure where. Was it a defect, a bad sensor, a short,
or some mis-wiring on our part? We were running out of motivation
and ideas and decided to reach out to the online enthusiast
community for help. We posted our problems on several tech
forums and asked for ideas. Then we sat back and hoped someone
out there would produce a solution.
The purple wire is the "TFI Start" circuit.
This circuit applies 12V to the TFI module upon cranking
and the computer in turn retards timing to facilitate
faster engine starting. Our goof resulted in the timing
being retarded continuously such that the engine wouldn't
run past 3500 rpm. |
After a couple weeks Wade
Chamberlain, who goes by the handle FFR Cobra on the Corral.net
and other forums posted a response which looked to us as being
the key to unleash this engine. He suggested that we likely
had one of the wires to the distributor TFI module connected
to a full-time 12V source, when in fact it should only receive
12V during cranking. He explained that this circuit in the
EFI wiring serves to retard timing while engine cranking for
faster starting. If the circuit is seeing 12V while the engine
is running in effect the timing is being retarded. This made
perfect sense, since in fact the 3500rpm break up felt more
like a rev limiter then it did a misfire or fuel starvation
issue. Wade also added that this is a common mistake when
guys convert older vehicles to fuel injection because it is
easy to assume that the only connection ever requiring 12V
during cranking only is the starter.
The next morning we moved the wire over to the starter side
of the ignition relay and fired the motor up. A single stab
of the accelerator pedal is all that it took to realize the
weeks of frustration were over. The motor reved beyond 3500
for the first time, and now we were in business.
To Mass-Flo's credit their instructions
clearly indicate that the purple TFI wire is supposed
to connect to a cranking 12V source. We even marked it
properly in the above image which we ran in Part II. However
we misinterpreted this to mean 12V during cranking and
running. Again, we assumed that there couldn't possibly
be a circuit, other than the starter, that needs 12V only
during cranking. My bad. |
Simply connecting the wire to the starter activation side
of the solenoid resolved the problem. |
|